Spicerack
Member
Alrighty. Here goes. This is for a Zongshen 140 kickstart only motor.
This is a bike I've got no history on, so don't know if it ever ran with this setup. Doesn't look like it's been changed about but you never know.
It runs terribly, popping and misfiring at idle with very occasional moment when it seems to run a bit better then carries on misfiring. It won't rev much at all above idle and tends to die when you try and rev.
Choke makes very little difference. Possibly a tiny bit better but still not good.
Cupping hand over air filter makes very little difference.
Changing pickup timing makes very little difference (I made it adjustable).
The timing light shows it is sparking at the "F" mark just advanced from TDC so about right?
Changed needle position and no discernible difference.
The only thing I haven't done is alter the mixture needle- 1.5 turns from bottom (factory setting).
Brand new NGK plug.
Carby cleaned and no problems.
Excellent compression- if kick start feel is to go by!
Valve clearances done.
No intake leaks.
Fresh fuel.
Cam timing is spot on the marks at TDC.
Earthing between engine, frame, cdi, coil etc is good.
The carby is one of those 22-26mm oval throat Mikuni's.
Main jet is 95, pilot jet is 15. I thought maybe a bit small?
So any ideas?
Symptoms of running stupidly lean?
Something wrong with the valve timing/seal?
Coil/CDI stuffed?
Stator problem?
Must admit I'm a bit stumped and am about to start buying new coil/cdi etc an go through the swapping process.
This is a bike I've got no history on, so don't know if it ever ran with this setup. Doesn't look like it's been changed about but you never know.
It runs terribly, popping and misfiring at idle with very occasional moment when it seems to run a bit better then carries on misfiring. It won't rev much at all above idle and tends to die when you try and rev.
Choke makes very little difference. Possibly a tiny bit better but still not good.
Cupping hand over air filter makes very little difference.
Changing pickup timing makes very little difference (I made it adjustable).
The timing light shows it is sparking at the "F" mark just advanced from TDC so about right?
Changed needle position and no discernible difference.
The only thing I haven't done is alter the mixture needle- 1.5 turns from bottom (factory setting).
Brand new NGK plug.
Carby cleaned and no problems.
Excellent compression- if kick start feel is to go by!
Valve clearances done.
No intake leaks.
Fresh fuel.
Cam timing is spot on the marks at TDC.
Earthing between engine, frame, cdi, coil etc is good.
The carby is one of those 22-26mm oval throat Mikuni's.
Main jet is 95, pilot jet is 15. I thought maybe a bit small?
So any ideas?
Symptoms of running stupidly lean?
Something wrong with the valve timing/seal?
Coil/CDI stuffed?
Stator problem?
Must admit I'm a bit stumped and am about to start buying new coil/cdi etc an go through the swapping process.