epod
Well-Known Member
- Joined
- Oct 26, 2006
- Messages
- 222
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G'day all, I recently did a port job on my yx klx style head on pitsterx4 160. First thoughts after first ride were unreal its flying pulling harder all through the rev range. I only got about half hours riding at home before packing up the bike to drive to lake's for the race last weekend. Entered in vets but managed to get 3 practice sessions in with vets china's and pro's. At the end of 6 laps the bike is still flying but oil is leaking onto the exuast and burning off. It seems to be leaking out the exuast port flange somehow and not going into the exuast just leaking down the outside of the exaust header only. I was only losing about ten mills of oil during a 5 lap race but it smoked alot as the oil burned on the pipe. I ran it all day like this and won the vets.
I have since taken the head off and cannot work out how it could be leaking at this point justoutside the exuast port on the outer edge of the flange as the does not seem to be any gap. Put it back together same problem.
I have noticed the casting on this head is very poor quality compard to the crf dirtmax head on my yx 150cc. Has this happed to anybody else out there.
Note most of the port work was to the inlet port just straitening the flow to the valve. as for the exuast I just cleaned it up a little. There is no oil leakage inside the ports at all and the motor is running clean and very fast. I still can't believe it. I have never seen a motor smoke so much from, oil leak and run for more than five miniutes. The head gasket is not blown.
Any ideas? Any body want to donate another head?
Peace ride on. DD
I have since taken the head off and cannot work out how it could be leaking at this point justoutside the exuast port on the outer edge of the flange as the does not seem to be any gap. Put it back together same problem.
I have noticed the casting on this head is very poor quality compard to the crf dirtmax head on my yx 150cc. Has this happed to anybody else out there.
Note most of the port work was to the inlet port just straitening the flow to the valve. as for the exuast I just cleaned it up a little. There is no oil leakage inside the ports at all and the motor is running clean and very fast. I still can't believe it. I have never seen a motor smoke so much from, oil leak and run for more than five miniutes. The head gasket is not blown.
Any ideas? Any body want to donate another head?
Peace ride on. DD